Good morning all!
I saw something like this once in my life, but was an over rev and over boosting together, the operator took off with 115% of power, and the Westgate remained closed, causing an over boost, and he had an variable pitch prop., but he kept the engine running for more than 5 minutes in this condition, after that, the engine lost power, the owner made an emergency land, no damages to aircraft or occupants, but the crankshaft got almost the same as yours, with a huge gap in the connecting road