Thank you for the information! I had the fluctuation before removing the check valves with the boost pumps. There is a serviceable filter at the boost pump-mine were terribly dirty (picture attached). Cleaning out the fuel pressure regulator, however, was the only thing that has lessened the fluctuations to near zero. Fluctuations came back after about 3 hours of flight of doing so the first time. Right before leaving Midwest, I went from almost a full psi swing in both directions, down to stable after cleaning out the regulator again (which didn't appear dirty), and not at 3 hours of flight yet to see if it comes back. Although the fluctuation only occurred with the left tank, that was the only "temporary" fix that worked. It's my hope the fluctuations do not come back. Happy to hear your fluctuation is currently not present.