UPDATE
First, I want to thank all responders for taking the time to comment. I really appreciate it. It really makes me think about all the perspectives.
This is what I actually since the last flight when I had the problem. Went back to my BUDS files that I did have and noticed that there some EGT error on Cylinder 1, not for the event, but before that. So I keep a new spare EGT prove handy and swapped it out. Additionally went back and cleaned all the EGT connections with contact cleaner. Blasted them.
I figure bad EGT probe/reading could trigger such an event.
During my climb out, during the event (low RPM at WOT and vibration), I noticed that the EGT's of cylinder 2 and 4 were noticeably lower. Not by much but noticeable. I gave the fuel tanks a heavy dose of sea foam to clean any fuel injectors that may be plugged.
Today we got 6 hours and it ran great. We are extra cautious with our flying and making sure airports are close by until we get more time.