Here’s some closure-I got my engine going again yesterday after several months of down time. I had several issues, and I’ll outline them in probable chronological order with solutions.
1. Rubber connecting the airbox to the 2/4 carb was dry rotted. (Replaced all rubber connected to the air box).
2. 2/4 carb was contaminated, plunger was gummed up and not allowing the carb to function-this meant only half the engine was working, and caused a wicked vibration (rebuilt both carbs).
3. Severe vibration from only half the engine working rattled loose the airbox on the 2/4 carb (replaced rubber, reinstalled carb, safety wired airbox to both carbs).
4. Vibration also broke the P-lead on the B lane ignition module (replaced connector beffort the break).